Date Flight time  Description 4.12.2007 2hours TT 100 h End of test. Going to strip the machine and make complete isnpection and after that build some interesting scale model with this kit.  3.,12.200. 2hours Just flying ....... 2.12.2007 2hours Just flying ....... 1.12.2007 2hours Just flying ....... 30.11.2007 2hours Just flying ....... 29.11.2007 2hours TT 90 h Just flying ....... 28.11.2007 2hours Just flying ....... 27.11.2007 2hours Just flying ....... 26.11.2007 2hours Just flying ....... 25.11.2007 2hours Just flying - working and polishing the conversion picture here  25.11.2007 2hours TT 80h Just flying ....... 24.11.2007 2hours Just flying ....... 23.11.2007 2hours Just flying ....... 22.11.2007 2hours Original muffler back, going to cut the new one at half to see whats in. :D Pictures folows soon..  21.11.2007 2hours  Just flying .......New mufler arived mounted and test.  But no power difference as I expected.  20.11.2007 0 Damaged  thread has been found at exhaust bolt. Had two options: To use repail helicoil or make the bigger thread.  19.11.2007 2hours TT 70h Lowered the skids - it was too high - hard to fit to car.  18.11.2007 2hours  Just flying ....... 17.11.2007 2hours  Quited electronic ignition at buyer requests. New stock coil mounted back.  16.11.2007 2hours  Just flying ....... 15.11.2007 2hours Just flying - going to test new position for generator 14.11.2007 2hours TT 60h Just flying ....... 13.11.2007 2hours Just flying ....... 12.11.2007 2hours Just flying ....... 11.11.2007 2hours Just flying ....... 10.11.2007 2hours Just flying ....... 9.11.2007 2 hours TT:50 hours Gasser definitely become  just as a trainer and an "everyday" machine. 8.11.2007 2 hours Just flying ....... 7.11.2007 2 hours Just flying ....... 6.11.2007 2 hours Now clutch better - endurance test started...  5.11.2007 2 hours Bussiness card added under cluth liner  4.11.2007 2 hours Just flying...... 3.11.2007  2 hours 3D heavy duty clutch installed. Looks all OK engine   need more RPM to get the clutch engaged. Clutch bell keep cold.  1.11.2007 1 hour  Only one hour today. After i refilled the tank third time and get airborne, the huge smoke cloud from clutch area appeared. So, the clutch is finally gone.. I though ...more here 31.10.2007 2hours Total time 35 hours. Nice fllights, ignition starting at 8 deg very smooth and no prob with temp. Ftar 35 hours I can honestly say that I have much less problems with the gasser than with the regulalar glow engine heli .  Not even seems like test period....  30.10.2007 2 hours  Ops.......there is so stupid and so confusing system on other marks of ignition! As far i found, only the Falkon ignition works in logical way.
The others works in a backwards !! The Falkon ignition has to be setup at 8 deg to start and run at idle. When the RPM increase, the advance and voltage gets higher level as well.. But the other marks needs to be setup to 25-30 deg, when the engine started, they move to 8-10 deg position and by increasing RPM they adjust the "advance" back to starting point... Very interesting........ 29.10.2007 2 hours More info googled - tested  the ignition from 8 to 40 degree. Result: As more ignition, than more is engine sharp but the temperature riese equally. Going to searach the best level for my heli. Looks like each heli need proper ignition setting??  28.10.2007 2 hours Palying with electronic igniton needs to find more about the settings.  27.10.2007 2 hours As I promissed yesterday, but it was much more intereting than i thought:) Read here.. Morning going to install  electronic ignition. Very interesting thing:)  26.10.2007 Workshop break time :) Today was taken out only the  R30 Out in shop to get the fans and make calibration tool all here  25 hours...  25.10. 2007 2 hours  Changed blades for carbones - much better response and perfect track.  24.10. 2007 2 hours  Strong wind today, but   the  gasser is not a microheli:) 
All OK nice day...  23.10.2007 2 hours So playing with the settings like in laboratory - spending hours checking all around and again:) Have here somebody tested how many RPM have to reach the rotor at 5 degree of pitch to get the heli airborne?? 
I did today - my wife measured the rotations with result 1230 RPM at + 11.  22.102007 2 hours I lowe  it! Palying with curves, it certainly flies very well and shows plenty of potential. It shows incredible value for money, and certainly out specs some more expensive machine as far as features go. I guess now it’s just a matter of burning more fuel and putting some time on it to see how it stands up!  21.10.2007 2 hours The generator pinion fail today. The generator axis is broken to 2 parts. Needs to be supported by bearing on the top as well. So, not OK, going to find other solution..  First inspection and upgrades read here 20.10.2007 2 hours TT: 15 hours done - inspection time.. First 3D on video Incredible power visibility etc...
Selling all glow birds and parts!.. Video here 19.10.2007 2 hours Tested tempreture with onboard temp gauge. Read here. Heli OK no problem. Looks like i can go ahead and set up the heli to D and try few basic 3D.  18.10.2007 2 hours Have made new front holder for canopy.  Now keeps well, no vibrations no problem. Used common raptor canopy holder. Foto here 17:10 2007 2 hours Air filter mounted - picture in gallery. Have less resistance, engine taking more amount of air. The H needle needs to be opened 1/4 more.  16.10 2007 2 hours Clutch works perfect increasing the fligt time. 
Going to test new canopy fotos here 15.10 2007 1 hour and bit (total 5)  All perfect the Cyclone and JR servos are completly resistent to HF frekvency from  plug cable. What io was waiting for, is the clucth description here 14.10.2007  1 hour Changed PPM JEti RX7 reciever to SPCM 
Chicken dancing at thotle servo apear. Solution here 12:10.2007  1 hour  Broken negative contact  in coil replaced with goped one 11.10.2007 1 hour Howering 10.10.2007 1 hour  Fist take off